I was up in the loft the other day and made a start on the North Side Station, the through line has been laid and is all wired up. Below view from the West end.
View from the East end.
Just 3 more points and some rail plus wiring to tack in now. As you can see I have been laying the wire as is my norm these days in electricians trunking with a removable top. Makes life so much easier for fault finding if any needed plus I can see the joins back to the panel hiden inside as well. I have been using the connectors from RS Stock No. 8837544 which have a push connection to hold the wires in place . Not sure how they would fare outside but I imagine would be Ok if placed inside a dry building or some other such place. There are 2 push ins per connector so the main wire from the pannel to the outside track goes to the outside screw terminal and subsidery wires to the track in the other one. The inside wire from the panel goes to a second connector to the inside screw terminal with the track wires heading out on the other one.
You can see that I have terminated the main wire from the pannel and run another out to the other end of the board. I also use the stripe for the outside rail and have splogged some white paint on the outer rails wires to help out keeping track of things. When the top is placed back on the jumble of wires beneath is lost. I tend to cut the top up some so that I have short pieces to put in place to keep things inside when wiring up.
Once that was all done I ran the set you can see with 3 carriages round the circuit a few times to see for any dodgy joints etc. A few issues came to the fore which will be attended to once all of the track is laid. However a puzzling one was a coach derailing on a trailing point on every pass. Looking at it from track angle it became clear that it was more of a decoupling that was causing the issue. As I do not have hooks on locomotives clearly it was the carriage and the following pic shows that the spring had weakened causing the hook to be low.
After removing the hook you can see the problem.
This coach and the others had been stored on a shelf in my tin shed so likely this hook had been pressed against the end wall and pushed the hook down eventually weakening the spring. This is something that can occure with badly packed stock and home made buffer stops that do not have space for the hook to sit in the correct manner. The resolution is quite simple, just turn the spring over and all is well again as seen below.
This pic shows just how the issue can be created.
Next time we should getbonto the rest of the track laid and wired up.